
Trouble with my 96' Sportster
#1
Posted 14 July 2009 - 09:55 AM
Issue 1: I never thought this was an issue until i started looking through the forum for issues related to the wear ring.
from a stop ill put the throttle about 80% forward and it will rev and then a second or two later it will feel like it would catch and then lift up and begin to plane, Ive read that its supposed to "jump out of the water"
Thoughts?
Issue 2: Driving around today towing, after we stopped to pull the tuber back in, when we started it back up and would go 80% throttle to get going, it wouldnt feel like it would rev as high and was EXTREMELY sluggish. so I limped it all the way back to the marinia. Looked into the back portion of impeller and it looked like gunk was in there. walked to the marina store to get a flash light, and ended up bumping into a sea doo mechanic, and he took a quick look, i just told him it looked like i sucked up something. I didnt mention anything to him about it being extremely sluggish.
He crawled under the boat (on the trailer at this point) and looked at it and said i def. sucked something up and the wear ring was toast! but the impeller looks perfect. (told me to take it to his shop and they could get to in in 3 weeks)
But I guess im really not 100% understanding what role the wear ring plays. so if that was to go bad, would that be a cause to this issue? or even issue number 1?
Thoughts?
Issue 3: I heard a humming noise, the sea doo guy looked at it and said the floater was up or open on the beilge pump. can someone explain that and a how to fix for that?
#2
Posted 15 July 2009 - 12:19 AM
Thanks in advanced for the help....
Issue 1: I never thought this was an issue until i started looking through the forum for issues related to the wear ring.
from a stop ill put the throttle about 80% forward and it will rev and then a second or two later it will feel like it would catch and then lift up and begin to plane, Ive read that its supposed to "jump out of the water"
Thoughts?
Issue 2: Driving around today towing, after we stopped to pull the tuber back in, when we started it back up and would go 80% throttle to get going, it wouldnt feel like it would rev as high and was EXTREMELY sluggish. so I limped it all the way back to the marinia. Looked into the back portion of impeller and it looked like gunk was in there. walked to the marina store to get a flash light, and ended up bumping into a sea doo mechanic, and he took a quick look, i just told him it looked like i sucked up something. I didnt mention anything to him about it being extremely sluggish.
He crawled under the boat (on the trailer at this point) and looked at it and said i def. sucked something up and the wear ring was toast! but the impeller looks perfect. (told me to take it to his shop and they could get to in in 3 weeks)
But I guess im really not 100% understanding what role the wear ring plays. so if that was to go bad, would that be a cause to this issue? or even issue number 1?
Thoughts?
Issue 3: I heard a humming noise, the sea doo guy looked at it and said the floater was up or open on the beilge pump. can someone explain that and a how to fix for that?
Issue 3: If the float switch is stuck up, there may be some debris holding it up. Try flushing the bilge pump and float switch with fresh water.
#3
Posted 15 July 2009 - 11:47 AM
Issue 3: If the float switch is stuck up, there may be some debris holding it up. Try flushing the bilge pump and float switch with fresh water.
Sorry about the NEWB question, but how do you flush the bilge pump?
#4
Posted 26 July 2009 - 11:39 PM
Sorry about the NEWB question, but how do you flush the bilge pump?
The best way is to remove it from the hull (should snap into and out of, a base attached to the hull. That said, I see mine is difficult to get at, you could just squirt it with a garden hose.
#5
Posted 28 July 2009 - 02:00 PM
Kevin Seeber
Kingsland Marine
Thanks in advanced for the help....
Issue 1: I never thought this was an issue until i started looking through the forum for issues related to the wear ring.
from a stop ill put the throttle about 80% forward and it will rev and then a second or two later it will feel like it would catch and then lift up and begin to plane, Ive read that its supposed to "jump out of the water"
Thoughts?
Issue 2: Driving around today towing, after we stopped to pull the tuber back in, when we started it back up and would go 80% throttle to get going, it wouldnt feel like it would rev as high and was EXTREMELY sluggish. so I limped it all the way back to the marinia. Looked into the back portion of impeller and it looked like gunk was in there. walked to the marina store to get a flash light, and ended up bumping into a sea doo mechanic, and he took a quick look, i just told him it looked like i sucked up something. I didnt mention anything to him about it being extremely sluggish.
He crawled under the boat (on the trailer at this point) and looked at it and said i def. sucked something up and the wear ring was toast! but the impeller looks perfect. (told me to take it to his shop and they could get to in in 3 weeks)
But I guess im really not 100% understanding what role the wear ring plays. so if that was to go bad, would that be a cause to this issue? or even issue number 1?
Thoughts?
Issue 3: I heard a humming noise, the sea doo guy looked at it and said the floater was up or open on the beilge pump. can someone explain that and a how to fix for that?
Kingsland Marine
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